Commentary about volunteering to overhaul the 200 hp LeRoi engine in a Whitcomb switch locomotive for a non profit museum. I got it running in 2009. TitanX Donated a new radiator core in 2011. Plymouth locomotive arrives 2014.
Sunday, May 24, 2009
Install the intake manifold
Hank and I went to the Museum Sunday May 24th to work on the Whitcomb engine. We had three objectives: mount the intake manifold, disassemble the air compressor head and build a frame to jack the hood up.
We worked on the water cooled intake manifold at home. The water jacket on the manifold was cracked due to freezing. I epoxied the cracks and Hank drilled out the rusted drain plug. The exhaust manifold has six connections to the exhaust ports, three connections for water cooling to the head, and four water connections to the intake manifold. The intake manifold has 4 water connections and connects to all three heads. Just about everything needed pried up, down or sideways to get the bolts started in. All connections had new gaskets. We noticed quite a bit of rust and scale in the water jacket of the exhaust manifold. We removed the stuck thermostat and tried to get as much rust out as possible.
Monday we took the cover off the air compressor valve chamber using instructions from Andy Szabo from Arizona Railway museum. The leather seal washer was hard and brittle. Two new ones were ordered. Hank spent quite a bit of time removing some black hard carbon like crap that was blocking about half of the exhaust port. All the valves were stuck and I could not get the exhaust valve out. The others will be disassembled and cleaned. I installed the Conrader unloader and cut a copper line to attach to the air compressor head.
Tuesday Hank and I sawed up some lumber to lift or support the hood while the radiator is repaired.
Friday, May 8, 2009
Exhaust manifold mounted
May 6,7,8. We got the water manifold, between the three blocks, on the right side of the engine on with neoprene gaskets. The water pump which drives the distributor and magneto was cleaned up at home and the timing was set. The water pump gear was carefully mated with the timing gear to have the spark occur at the correct time (20 degrees before top dead center we hope!). James was working on the 25 ton GE and Ryan showed up. They helped me get the 6 ft long exhaust manifold mounted on the engine. It is still loose because it has to line up, and bolt up to several other castings on the head and intake manifold. We are working on the intake manifold to drill out the pipe plugs and install ball valves to drain the water. The conrader unloader is being disassembled and cleaned.
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